I'm trying to run 3rd gen Toyota 1G engine with RusEFI, and I am mostly successful, apart from small issues with trigger, and the show-stopper -> TPS and PPS.
This throttle body has a DC motor, double TPS, and PPS mounted, the setup is very similar to BMW with M52TU motor.
Both TPS and PPS have exactly the same spec, the problem is that as I can see RusEFI expects both sensors to have full linear range covering all angles. Unfortunately only the first sensor is covering the full range, second one is offset, and above about 70 degree it maxes out as in the photo attached. In the logs it can be seen that when I am depressnig the pedal in the linear range it's working good, but when I go past the "kickdown switch", I get the pedal error.
Worse situation is with TPS, it's showing the "Tps1 sensor inconsistent" all the time in RusEFI console, also log attached with ETB Calibration ran few times. A little bouncing can be seen after calibration because I forgot to turn off PID regulator...
Is it possible to get this to run?
